Refinery Vapour Control – Maintenance Turnaround – Emissions Control and Degassing

Executive Summary

When a major refinery took its hydrogen plant offline for turnaround, fuel gas consumption dropped dramatically — creating up to 3 million SCFD of excess fuel gas vapor control problem that could not be routed to the flare without violating the state and federal emission controls laws.

Envent engineered and deployed a parallel high-pressure thermal oxidation system with >99.99% DRE, operating under an approved Alternative Monitoring Plan (AMP). The result: zero flaring, zero incidents, and the fastest hydrogen plant turnaround in the refinery’s history.

Project At A Glance

  • Location: U.S. Gulf Coast Refinery
  • Challenge: 3 Million SCFD Excess Fuel Gas During H₂ Plant Turnaround
  • Solution: Dual-Stream High-Pressure Thermal Oxidation with AMP
  • Outcome: Zero Flaring, Zero Incidents, Record Turnaround Speed

The Challenge: Excess Fuel Gas During Hydrogen Plant Shutdown

Taking the hydrogen plant offline reduced refinery fuel gas demand, leaving up to 3 million SCFD of excess high-pressure fuel gas with no sink.

Key Constraints Regulatory Compliance The EPA Refinery Sector Rule (RSR)40 CFR §63.670(o) prohibits routine flaring during MSS events and requires ≥98% destruction efficiency with approved monitoring. Uncontrolled releases could trigger fines and Title V deviations.

Operational Demands High-pressure, variable-composition fuel gas required precise pressure control and detonation protection without delaying the critical-path hydrogen plant schedule.

Safety & Emission Risks Routing to the flare would exceed capacity and visibility limits; carbon or recovery alone could not handle the volume safely.

Official EPA Resources

Envent’s Engineered High-Pressure Thermal Oxidation Solution

Envent conducted a detailed pressure-loss study and PHA to design a parallel dual-stream system:

Treatment Process & Destruction Details Pressure Control Custom regulator systems sized for two high-pressure streams, maintaining safe delivery to oxidizers.

Safety Enhancements Specialty auxiliary detonation arrestors + control/isolation valves for unforeseen conditions.

Emission Controls and Vapour Destruction from pipe and vessels with upgraded controls and real-time analyzers delivered >99.99% DRE under the approved AMP.

The system operated continuously with 24/7 Envent operators, handling the full 3 million SCFD load.

Proven Benefits: Zero Flaring, Record Turnaround

Benefit Project Impact
Emissions Compliance Zero flaring, zero fines, full RSR/MACT 2 & AMP compliance
Destruction Efficiency >99.99% vs. flare’s typical 95%
Turnaround Schedule Fastest hydrogen plant turnaround in refinery history
Safety & Reliability Zero incidents despite high-pressure, variable fuel gas
Operational Flexibility Parallel streams + custom controls handled all upsets

The refinery completed the hydrogen plant turnaround faster than ever before, generating above-average profits for the year.

Planning a hydrogen plant or fuel gas imbalance turnaround? Get your Free EPA RSR / AMP Compliance Review & Quote today. Call Envent’s Turnaround Division at 888-997-9465 or email [email protected] — we keep your flare off and your schedule on track.